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|| FILT_GratingCharact_20070222_03.tm
FILT_GratingCharact_20070222_04.tm
FILT_GratingCharact_20070222_05.tm
FILT_GratingCharact_20070222_08.tm
FILT_GratingCharact_20070222_09.tm
FILT_GratingCharact_20070222_10.tm
FILT_GratingCharact_20070222_11.tm
FILT_GratingCharact_20070222_12.tm


  
* Nominal:
   * Stability after homing not reproducable
      * 22nd afternoon: 6 homings followed by stable situation (10 digits noise
        peak-to-peak)
      * 22nd evening: no single home followed by stable situation (60 peak-to-peak)
   * Disabling/enabling the controller improves the stability
      * Disable : always brought the noise to few (3-4) digits peak-to-peak.
      * Enable : always brought the noise te 10 digits peak-to-peak
      * But a new homing or movement to extremes of the range degrades the stability
        again to 60 peak-to-peak.
   * High torque
      * Disabling the controller at extreme positions in the range produces
        large amplitude swing-back (plot will follow)
   * Friction ?
      * Several disablings of the grating controller at position 500000 produced
        swing-backs in different directions. To be checked if this is correllated
        with the direction we come from (we have the data, looking into that now)

* Redundant:
   * On the 21st in the afternoon and evening, disabling the grating controller
     in the redundant chain did not reduce the oscillations. During a 40 minutes
     measurement where we left the controller disabled, we collected enough data
     to have a good S/N in the hall sensor readout - in the plots in attachment you can
     see that a significant peak is seen in hall B and the inductosyn readout around
     8.4Hz. Hall A was in a flat part of the sine curve.
     (FILT_GratingCharact_20070221_26_curPosHallAFft.png

FM ILT Grating control analysis

Measurements (2nd FM ILT run)

|| FILT_GratingCharact_20070222_03.tm FILT_GratingCharact_20070222_04.tm FILT_GratingCharact_20070222_05.tm FILT_GratingCharact_20070222_08.tm FILT_GratingCharact_20070222_09.tm FILT_GratingCharact_20070222_10.tm FILT_GratingCharact_20070222_11.tm FILT_GratingCharact_20070222_12.tm

* Nominal:

  • Stability after homing not reproducable
    • 22nd afternoon: 6 homings followed by stable situation (10 digits noise
      • peak-to-peak)
    • 22nd evening: no single home followed by stable situation (60 peak-to-peak)
  • Disabling/enabling the controller improves the stability
    • Disable : always brought the noise to few (3-4) digits peak-to-peak.
    • Enable : always brought the noise te 10 digits peak-to-peak
    • But a new homing or movement to extremes of the range degrades the stability
      • again to 60 peak-to-peak.
  • High torque
    • Disabling the controller at extreme positions in the range produces
      • large amplitude swing-back (plot will follow)
  • Friction ?
    • Several disablings of the grating controller at position 500000 produced
      • swing-backs in different directions. To be checked if this is correllated with the direction we come from (we have the data, looking into that now)

* Redundant:

  • On the 21st in the afternoon and evening, disabling the grating controller
    • in the redundant chain did not reduce the oscillations. During a 40 minutes measurement where we left the controller disabled, we collected enough data to have a good S/N in the hall sensor readout - in the plots in attachment you can see that a significant peak is seen in hall B and the inductosyn readout around 8.4Hz. Hall A was in a flat part of the sine curve.

      (FILT_GratingCharact_20070221_26_curPosHallAFft.png

Herschel: FmIltAnal/GratingControlloop (last edited 2009-07-15 14:32:36 by localhost)